Laboratory investigation of dowel bars’ misalignment using pull-out test | ||
Al-Qadisiyah Journal for Engineering Sciences | ||
Volume 14, Issue 4, December 2021, Pages 201-204 PDF (377.48 K) | ||
Document Type: Research Paper | ||
DOI: 10.30772/qjes.v14i4.853 | ||
Authors | ||
Basim H. Al-Humeidawi* 1; Parthasarathi Mandal2 | ||
1Roads and Transport Department, College of Engineering, University of Al-Qadisiyah, Iraq | ||
2University Lecturer, School of Mechanical Aerospace and Civil Engineering, University of Manchester, M13 9PL, Manchester, UK | ||
Abstract | ||
Joint lockup due to dowel misalignment significantly affects joint and concrete pavement performance by causing joint distresses. The current paper presents an experimental study to assess the effectiveness of standard pull-out test in the evaluation of dowel misalignment effect on joint lockup of Jointed Plain Concrete Pavement (JPCP). The tests were conducted at two different ages of concrete ; 3 and 28 days. The results showed that the standard pull-out test or individually pulling of misaligned dowels cannot reflect the realistic defect of dowel misalignment. It also showed that the vertical orientation of misaligned dowel bars during the concrete casting reduces the pull-out load due to more distance from the exposure surface. Another observation was for all specimens, the pull-out load increases with an increase in concrete age. | ||
Keywords | ||
Concrete pavement; Pull-out; Dowel misalignment; Experimental test | ||
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